Tackling Print Adhesion Challenges with My Satin Sheet

The first sheet became a wall-mounted canvas for puzzle pieces with glued magnets (Einstein Non-Repeating Tile by Triple G Workshop).

In April, I eagerly invested $58.05 in an original double-sided satin powder-coated spring steel sheet, shipping included. Anticipating seamless printing, I was met with frustration when I couldn’t get my prints to adhere. Despite trying a plethora of adhesion solutions—painter’s tape, kapton tape, masking tape, purple glue stick, regular glue stick, scouring, dishwashing liquid, alcohol, and acetone—nothing seemed to work. I reluctantly returned to printing on a smooth sheet, clinging to the hope that a breakthrough was imminent. I explored various avenues to overcome the adhesion challenge, but even popular remedies like hairspray, with its airborne ingredients like Carboxymethylcellulose, Denatured alcohol, Hydrofluorocarbon Polyvinyl, Propylene glycol, and Polyvinylpyrrolidone, felt like an uneasy compromise. Discovering a reliable solution became my mission, as depending on hairspray posed its own set of problems.

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The Missing Piece of My Extruder Upgrade

Squeaking sounds were coming from my CR-10 Mini for months until I realized the cause. It was the timing belt; x-axis belt to be specific. I was hoping that all I needed to do was look for a CR-10 Mini replacement belt online and change the belt. I felt I would not have an issue with the process after watching two videos on Creality’s YouTube channel. The exact length of belt I needed was not readily available anywhere, meaning I would need to cut and crimp the belt myself. That was not something I was looking forward to doing. At the time, I was unaware of how essential timing belts were to obtaining good prints.

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Save Heat Energy Printing PLA During Summer Months

I designed a coffee table but I dreaded printing parts for it as I didn’t want to create a heat source in my living space during the early dog days of summer. The parts were to be printed on my Prusa MK3s+. The power supply unit (PSU) was on the outside of the enclosure I am building for the printer and I have noticed that it often becomes practically too hot to touch.

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Solution to Resume after Pause Problem

After installing a Microswiss Direct Drive extruder, I had one issue – the print end would not return to its last position after pressing pause. Since I did not use the pause feature often, I was not in a hurry to find a solution. However, I started to really miss being able to make multicolor prints. I finally contacted Microswiss and asked for help. A couple of weeks after back and forth emails, a super-knowledgeable and conscientious person named Paul found a solution. It was a retraction issue in the slicer.

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Installation Notes – CR10 Mini – 2nd Z-Axis

There are two reasons I installed a second z-axis; one reason was to balance the weight of a direct drive extruder I planned to install. The other reason was to balance the weight of the x-axis in general. I noticed in December that the axis was lower on the right side of the machine by about 4 mm. Considering that my first 3D printer was about 13 inches wide with dual z-axes, I was always leery about having a printer with a wider width and one z-axis. I suppose this upgrade was inevitable.

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